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Wyświetlanie 1-2 z 2
Tytuł:
Application of Trickling Filter and Vertical Flow Constructed Wetland Bed to Treat Sewage from Craft Brewery
Autorzy:
Dąbrowski, Wojciech
Karolinczak, Beata
Powiązania:
https://bibliotekanauki.pl/articles/124568.pdf
Data publikacji:
2019
Wydawca:
Polskie Towarzystwo Inżynierii Ekologicznej
Tematy:
craft brewery
sewage treatment
trickling filter
vertical flow constructed wetland
Certyd
Opis:
In Poland, as well as worldwide, an increase in craft beer production can be observed. In the last several years, more than 150 of such breweries have appeared and according to Polish Brewery Association, their number might ultimately reach 500. Many of them emerge in the areas with no access to a central sewerage system so they have to solve the problem of waste management on their own. The article presents the results of research on the possibility of using a hybrid system for biological treatment of sewage from craft breweries. The sewage came from a craft brewery Waszczukowe located in the Podlaskie province. A laboratory scale model consisted of a trickling filter (TF) (research model Gunt CE701e) and vertical flow constructed wetland (SS-VF). Innovative filling (Certyd produced by LSA company) of TF and SS VF was applied. The conducted study included determining the changes in the sewage parameters during hybrid treatment, as well as TF and SS VF efficiency separately. The aim of the research was to show the possibility of treating sewage to a point when it was possible to discharge it to a receiver, in compliance with the Polish legal regulations. The research results might be used in designing a treatment system or sewage pretreatment in craft breweries. The average efficiency of TF operating with 100% recirculation was 76% for BOD5, 80% for COD, 26% for TN and 34% for TP, while the total treatment efficiency of a hybrid system (TF and SS-VF) was 98%, 98%, 72% and 77%, respectively. The load of TF during operation with recirculation was on average 0.38 kg BOD5 m-2d-1, 0.57 kg COD m-2 d-1. The load of SS-VF was on average 0.09 kg BOD5 m-2 d-1 and 0.12 kg COD m-2d-1. The obtained results of hybrid treatment permitted to discharge the sewage to the receiver.
Źródło:
Journal of Ecological Engineering; 2019, 20, 9; 211-217
2299-8993
Pojawia się w:
Journal of Ecological Engineering
Dostawca treści:
Biblioteka Nauki
Artykuł
Tytuł:
Treatment of Craft Brewery Sewage with SS VF and FWS Constructed Wetland – Lab Scale Experiment
Autorzy:
Dąbrowski, Wojciech
Karolinczak, Beata
Malinowski, Paweł
Lech, Magrel
Powiązania:
https://bibliotekanauki.pl/articles/2069918.pdf
Data publikacji:
2021
Wydawca:
Politechnika Koszalińska. Wydawnictwo Uczelniane
Tematy:
craft brewery
sewage treatment
constructed wetlands
subsurface flow system
surface flow system
Opis:
The problem of wastewater treatment from craft breweries emerged in Poland about 10 years ago when an increase in the number of small breweries was observed. Plants located in small towns are forced to solve the problem on their own. One of the possibilities is to use low-cost technology of constructed wetlands with subsurface and surface flow. The purpose of the research was to test the possibility of effective treatment of sewage from a craft brewery in a lab-scale research installation and to determine the parameters for designing a real scale plant. Wastewater from the Waszczukowe brewery was used in the study. The research system consisted of a retention and aeration tank, SS-VF subsurface flow and FWS surface flow beds. An innovative Certyd filling produced by LSA company was used. The high efficiency of SS-VF bed and the entire research system was found. The removal efficiency in SS VF was on average 89.7% for BOD5, 90.5% for COD, 54.6% for TN and 52.1% for TP. For whole treatment it was respectively 97.1%, 96.7%, 72.6% and 61.3%. A high organic matter removal effect was found for the SS-VF bed (87.1 g BOD5g m-2 d-1) and a relatively low for the FWS (3.0 BOD5g m-2 d-1). The study confirmed the need for plant design based on hydraulic load and required load removed per unit area.
Źródło:
Rocznik Ochrona Środowiska; 2021, 23; 290--300
1506-218X
Pojawia się w:
Rocznik Ochrona Środowiska
Dostawca treści:
Biblioteka Nauki
Artykuł
    Wyświetlanie 1-2 z 2

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